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Kennedy Space Center - Culvert
Rehabilitation
The
Kennedy Space Center is a unique facility and an extremely
difficult one to maintain. Built between 1949 and 1963,
primarily on Everitt Island, all but operational areas are
designated as a wildlife refuge, containing over 500 species of
birds, reptiles, and animals, many of them on the endangered
spices list. The center runs 34 miles north to south and is
10 miles at its widest point. The center averages 5 ftp
about sea level, and contains 157 miles of paved roads and 87
mile of dirt or gravel roads.
Operating this high tech center and adhering to deadlines and
launch schedules while maintaining harmony with the environment
is no easy task for NASA Center Director Robert Crippen nor the
base operations contractor, EG & G Florida. Special
Maintenance headaches exist in a facility that must work around
launch deadlines and obtain environmental approval for literally
every maintenance problem that affects drainage, soil,
disturbance or removal. The center's infrastructure and
aging highways built in the 1940 to 1970 period are subject to
severe loads caused by heavy equipment, the never ending tour
buses that are a part of one of America's most popular
attractions, heavy fuel trucks, and a continuous stream of
traffic. Roads and culverts are aging and require a lot of
maintenance. The center is faced with tight budgets that
are constantly reviewed to keep costs low. Base operations
are managed under contract by EG & G Florida, a subsidiary of EG
& G Inc. EG & G is responsible for all building and
grounds maintenance including roads and railroads, security,
even fuel handling. Rodger Sorey,
branch manager for EG & G, has been at the center 32 years.
He and his staff must be innovative in highway maintenance.
"We need products and maintenance procedures that reduce costs
and make roads last longer," states Sorey. "We need
product maintenance procedures that reduce costs and make roads
last longer," sates Sorey. "Maintenance must be
considerate of the environment since we work in the center of a
national wildlife preserve. Silt runoff into the waterways
must be avoided." The culverts are a special problem.
Both bituminous coated corrugated mental and concrete culverts
are 35 to 50 years old and many have reached the end of their
useful life. Because of security considerations and
difficult time schedules, EG & G and its on-base road
subcontractor, USIA, do the majority of their own maintenance
work. Occasionally specialized work is bid and let to
outside contractors. Culverts a Special Problem
Each year the center is forced to replace a
growing number of aging culverts.
Once a road is cut open to replace a culvert, the road
invariably settles for three to for years no matter how well the
fill is compacted, resulting in a series of patches. Each
culvert replacement must be considered to determine how
dewatering or siltation would affect the environment.
Dewatering and building a stable base in swamp-like environment
is quite a challenge. To prevent danger to workers, the
cut must be tapered back to a 2 or 3 to 1 slope, resulting in a
wide, deep hold. Excavations must be well below the
culvert bottom to build a stable base for the replacement
culvert. This requires deeper than normal excavations.
In the fall of 1994, Sorey and 8000 Departments engineer Andy
Minor decided to try a cost saving alternative to culvert
replacement that would not disrupt base traffic flow nor disturb
the environment. "Culvert Renew" a profile wall, high
density, high molecular weight culvert liner was chosen to
rehabilitate two test culverts. "Culvert Renew" is
manufactured by Poly Systems Inc. of Steelville, Missouri.
The liner has a 100-year design life with very high abrasion and
chemical resistance. The decision to use this material
instead of other liners or polyethylene pipes was based on three
factors:
The liner has a minimum pipe stiffness of 46 psi
in all sizes. This high pipe stiffness gives a great
deal of resistance to deflection.
It has threaded ends for a
positive joint that will not pull apart while winching it
through offsets, and the joint is soil tight.
The linter is manufactured
from a premium grade resin that is HDB rated (PE 3408).
It has very high environmental stress crack resistance to
stand up to the gouging and abuse it will recieve when being
inserted in a culvert.
Twin 54-in corrugated metal
culverts were chosen for the test. The culverts were
severly rusted out and on one culvert the bands had bulled
apart, creating a severe wash-out on the downstream side that
caused the headwall to drop. Both shoulders, which are
approximately 20 to 25 feet wide, had experienced severe erosion
iorated culvert. The road itself was in danger of
collapse. The liner chosen had a 47 .47in OD with a 42in
ID. Even though the liner was smaller in size, it would
still give 116 percent of the original flow due to the improved
manning factor. Emergency Intervenes
However, before the work could begin on the
culverts that had been chosen to launch area and the primary
road used by the large double-decker tour buses collapsed and
was given immediate priority to repair or replace. The
twin culverts under the collapsed road were 42in diameter and
were installed over 35 years ago. Both concrete and
bituminous coated metal culverts were deteriorated due to age,
heavy traffic loads, and brackish water. The only liner
size that was immediately available was 40.65in OD with a 36in
ID. Normally this size would have been unacceptable as a
10 percent clearance is usually required to ensure that the
liner would fit through offsets and deterioration in the host
culvert pipe. However, due to the emergency, it was
decided to use the pipe on hand since the collapsed area would
have to repaired in any event, and a point excavation could be
easily made. Pulling heads were made
for the pipe by the company. The design is a pie-shaped
wedges out of the liner and pulling the nose cone to help the
pipe through any offsets. Due to the extremely tight fit,
a rear pulling device was designed by EG & G manager Sorey
so a cable could be run through the liner pipe and the pipe
pulled from both the front and the rear.
Unusual Hazard
First the culvert
was cleaned and the bituminous coating removed where
possible. The cleaning was accomplished with high pressure
washers. Before the cleaning could begin, the "local
residents" had to be induced to vacate the culvert. In one
culvert, a 6.5ft alligator was chased out, but in the other
culvert a 3ftp baby alligator was very difficult to chase away.
Obviously used to people, and perhaps even fed by the local base
personnel, every time he was chased away he would come right
back. However the high pressure cleaner scared him and he
decided to vacate on the run. The work crews always were
quite careful when first approaching a culvert, as an alligator
is very fast in the first 10 to 20 ftp, and can even catch a dog
who gets too close. After the
culvert was cleaned and the nose cone attached to the pipe, the
insertion was started. Two winch trucks were used to pull
the pipe from both the nose and the rear of the liner. The
first 40 ftp of liner went in the culvert without too many
problems. The next liner section was then rolled down into
the ditch and the sections joined together using nylon strap
slings tied loosely around the pipe with a long bar, then
twisted through the pipe. Since the sections of the liner
were 40ft in length and quite heavy, it took two two-man crews
to screw it together. it was easier to start the pipe
threads if the rear puller exerted a small amount of pressure to
pull the pipe tight against the first section while the crews
twisted the section to be joined. When both pipe sections
were in place, the crews were able to join the two sections in
about 15 minutes. With the sections
of pipe joined, the insertion process was started again.
this time, however, the winch trucks were unable to pull the
liner through a deteriorated section of the culvert. A
Gradall bucket crane was then positioned above the culvert,
partially on the road and partially on the road and partly on
the shoulder. A choke chain was looped around the pipe and
the crane's hydraulic arm was used to help pull the liner into
the culvert. The wooden rear puller plate, which was made
from four pieces of 3/4in plywood, cracked in half and wrinkled
the threads on the end of the pipe, but finally the liner went
all the way into the culvert. On the
second culvert the same insertion procedure was used with the
expectation that the rear wooden pulling plate was replaced with
a metal one, and a Caterpillar tractor was used to replace the
smaller winch truck. Since space was not a factor it was
decided to join the two liner section along the roadway.
Once joined, the 80ft section was rolled down into the ditch and
the cables, the pulling head, and rear pulling plate were
attached. Insertion in the second culvert was anticipated
to be more difficult as the top of the culvert was partially
missing, and a point excavation at the collapse are was used to
pull the top of the deteriorated culvert up so that the liner
could get through. When the liner reached the area of the
collapse, the 1 1/3in clearance was not sufficient to allow it
to pass though the partially collapsed culvert. Again the
Gradall bucket crane was used to help force the liner into the
culvert. The pipe was deformed about four inches before it
finally freed itself and passed though the collapse area.
The work crew was amazed at the abuse that the liner received by
forcing it though the culvert, and came to the conclusion that
it really is almost indestructible. The final section of
the pipe was then added and pulled though the culvert.
The entire operation for lining the two culverts had taken a day
and a half. This unusually long installation time was due
to the collapsed culvert and the small amount of clearance
between the liner and the culvert. Had the normally
recommended size of liner been available, the time of insertion
would have been less than two hours for both culverts and
cleaning time would have been reduced. Once the liner
pipes had been cut off at the headwall, a hydraulic grout was
used to seal the annular space at the ends of the liner to
prevent any soil migration through the space. The
collapsed area was then filled, compacted, and a new six inch
cap put on the collapsed area. The road was immediately
opened again to traffic, much to the relief of all concerned.
Back To The Planned Test
When the emergency was
over, attention turned to the original demonstration culverts.
The section of headwall that had cracked and dropped had to be
removed to allow for the "Culvert Renew" liner to be inserted.
Also, the collapsed area of pipe on the shoulder was removed.
A base fire truck was then used to flush out approximately 19
inches of mud in it. The pipe was then assembled on the
bank of the downstream ditch, which was more like a small lake
than a ditch. In all, 90Ft of the liner pipe was
threaded together then rolled down the bank with a rope attached
to the nose cone to guide it into the culvert. The rope
was removed and replaced with the pulling cable. This time
the Caterpillar tractor easily pulled the liner completely
though the deteriorated culvert in less than 20 minutes.
The second culvert was assembled on the bank and pulled though
the culvert easily in similar fashion. Once the liners had
been inserted, the broken headwall was repaired and since the
original culvert was in such poor condition, the annular space
was grouted to prevent any road collapse due to soil migration.
According to Sorey, "relining culverts rather than replacing
them has server advantages. Cost savings average about 65
percent versus replacement. With the age of the base's
culverts, many will have to be replaced or relined, so cost
savings become a significant consideration. It is also
important not to have to disrupt traffic on the heavily traveled
roads. Detours are very difficult since in many cases there is
no convenient detour route. Closing some roads on the
congested base would have been next to impossible. This
problem is solved by relining rather than replacing the
culverts. "Calculating the flow gave us a big surprise
too. The manning factor of the polyethylene liner is much
better than either concrete or corrugated metal. In many
cases flow capacity remains the same as the original culvert and
often flows can be increased by the lining procedure.
"Environmentally we are better off any time we do not have to do
major excavations. In our environment with brackish water
and heavy traffic loads, the 100 year design life is a big plus.
Overall, I would have to say we were pleased with the lining
procedure and as required, hope to do many more in the future."
The proceeding article was based on information
submitted by Steve Campbell of Poly Systems, INC., and
republished by Public Works issue of March, 1995.
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